Alam Md Shafiq, Sharma D K, Sehgal V K, Arora M, Bhatia S
Department of Processing and Food Engineering, Punjab Agricultural University, Ludhiana, 141004 India.
J Food Sci Technol. 2014 Nov;51(11):3476-81. doi: 10.1007/s13197-012-0863-0. Epub 2012 Oct 16.
A fully mechanized honey heating-cum-filtration system was designed, developed, fabricated and evaluated for its performance. The system comprised of two sections; the top heating section and the lower filtering section. The developed system was evaluated for its performance at different process conditions (25 kg and 50 kg capacity using processing condition: 50 °C heating temperature and 60 °C heating temperature with 20 and 40 min holding time, respectively) and it was found that the total time required for heating, holding and filtration of honey was 108 and 142 min for 25 kg and 50 kg capacity of machine, respectively, irrespective of the processing conditions. The optimum capacity of the system was found to be 50 kg and it involved an investment of Rs 40,000 for its fabrication. The honey filtered through the developed filtration system was compared with the honey filtered in a high cost honey processing plant and raw honey for its microbial and biochemical (reducing sugars (%), moisture, acidity and pH) quality attributes. It was observed that the process of filtering through the developed unit resulted in reduction of microbes. The microbiological quality of honey filtered through the developed filtration system was better than that of raw honey and commercially processed honey. The treatment conditions found best in context of microbiological counts were 60 °C temperature for 20 min. There was 1.97 fold reductions in the plate count and 2.14 reductions in the fungal count of honey processed through the developed filtration system as compared to the raw honey. No coliforms were found in the processed honey. Honey processed through developed unit witnessed less moisture content, acidity and more reducing sugars as compared to raw honey, whereas its quality was comparable to the commercially processed honey.
设计、开发、制造了一种全机械化蜂蜜加热兼过滤系统,并对其性能进行了评估。该系统由两部分组成:顶部加热部分和下部过滤部分。在不同工艺条件下(分别使用25千克和50千克容量,加工条件为:加热温度50℃和60℃,保温时间分别为20分钟和40分钟)对所开发的系统进行了性能评估,结果发现,无论加工条件如何,25千克和50千克容量机器的蜂蜜加热、保温和过滤所需的总时间分别为108分钟和142分钟。该系统的最佳容量为50千克,制造该系统的投资为40,000卢比。将通过所开发的过滤系统过滤的蜂蜜与在高成本蜂蜜加工厂过滤的蜂蜜以及生蜂蜜在微生物和生化(还原糖(%)、水分、酸度和pH值)质量属性方面进行了比较。观察到通过所开发的装置进行过滤的过程使微生物数量减少。通过所开发的过滤系统过滤的蜂蜜的微生物质量优于生蜂蜜和商业加工蜂蜜。在微生物计数方面发现最佳的处理条件是60℃温度下保温20分钟。与生蜂蜜相比,通过所开发的过滤系统加工的蜂蜜的平板计数减少了1.97倍,真菌计数减少了2.14倍。在加工后的蜂蜜中未发现大肠菌群。与生蜂蜜相比,通过所开发的装置加工的蜂蜜水分含量、酸度较低,还原糖较多,而其质量与商业加工蜂蜜相当。