Chatterjee Pritha, Ghangrekar M M
Department of Civil Engineering, Indian Institute of Technology, Kharagpur 721302, India E-mail:
Water Sci Technol. 2017 Sep;76(5-6):1234-1242. doi: 10.2166/wst.2017.269.
A pilot-scale upflow anaerobic sludge blanket-moving bed biofilm (UASB-MBB) reactor followed by a high-rate algal pond (HRAP) was designed and operated to remove organic matter, nutrients and pathogens from sewage and to facilitate reuse. For an influent chemical oxygen demand (COD) concentration of 233 ± 20 mg/L, final effluent COD was 50 ± 6 mg/L. Successful biomass granulation was observed in the sludge bed of the upflow anaerobic sludge blanket (UASB) reactor after 5 months of operation. Ammonia removal in HRAP was 85.1 ± 2.4% with average influent and effluent ammonia nitrogen concentrations of 20 ± 3 mg/L and 3 ± 1 mg/L, respectively. Phosphate removal after treatment in the HRAP was 91 ± 1%. There was a 2-3 log scale pathogen removal after treatment in HRAP with most probable number (MPN) of the final effluent being 600-800 per 100 mL, which is within acceptable standards for surface irrigation. The blackwater after treatment in UASB-MBBR-HRAP is being reused for gardening and landscaping. This proper hydro-dynamically designed UASB reactor demonstrated successful granulation and moving bed media improved sludge retention in UASB reactor. This combination of UASB-MBB reactor followed by HRAP demonstrated successful sewage treatment for a year covering all seasons.
设计并运行了一个中试规模的上流式厌氧污泥床-移动床生物膜(UASB-MBB)反应器,随后是一个高速藻类塘(HRAP),以去除污水中的有机物、营养物质和病原体,并促进污水回用。对于进水化学需氧量(COD)浓度为233±20mg/L的情况,最终出水COD为50±6mg/L。运行5个月后,在上流式厌氧污泥床(UASB)反应器的污泥床中观察到成功的生物质颗粒化。HRAP中的氨去除率为85.1±2.4%,进水和出水氨氮平均浓度分别为20±3mg/L和3±1mg/L。HRAP处理后的磷酸盐去除率为91±1%。HRAP处理后病原体去除对数为2-3个数量级,最终出水的最可能数(MPN)为每100mL600-800个,这在地表灌溉的可接受标准范围内。UASB-MBBR-HRAP处理后的黑水正在用于园艺和景观美化。这种水力设计合理的UASB反应器展示了成功的颗粒化,移动床介质提高了UASB反应器中的污泥保留率。这种UASB-MBB反应器与HRAP的组合在一年的所有季节都成功地进行了污水处理。