School of Chemical and Environmental Engineering, China University of Mining and Technology (Beijing), Beijing, 100083, PR China; State Key Laboratory of Coal Resource and Safe Mining, China University of Mining and Technology (Beijing), Beijing, 100083, PR China.
School of Chemical and Environmental Engineering, China University of Mining and Technology (Beijing), Beijing, 100083, PR China; State Key Laboratory of Coal Resource and Safe Mining, China University of Mining and Technology (Beijing), Beijing, 100083, PR China.
Water Res. 2020 Sep 15;183:116090. doi: 10.1016/j.watres.2020.116090. Epub 2020 Jun 29.
In this study, the performance of catalytic ozonation in the treatment of bio-treated coking wastewater (BCW) using pilot- and full-scale systems was investigated. Additionally, the removal efficiency of organic pollutants from BCW, the deactivation mechanism of MnCeO/γ-AlO, and backflushing optimization for in-situ catalyst regeneration, which have not been previously investigated, were analysed. Results of the 12-month pilot scale experiments showed that catalytic ozonation resulted in the effective removal of organic pollutants when backflushing was applied as an in-situ catalyst regeneration strategy. The effluent chemical oxygen demand (COD) content decreased from 150 to 78 mg L, and remained below a discharge limitation of 80 mg L, and the stable COD removal efficiencies (from 56.0% to 47.9%) indicated that catalyst deactivation, which primarily resulted from the deposition of inorganic salts on the surface of the catalyst that limited interaction between ozone and active sites and/or prevented electrons transfer, was primarily inhibited by backflushing. The catalyst regeneration via in-situ air- and water-backflushing was attributed to the scrubbing, collision, and/or the loosing effect. Additionally, in the full-scale experiment, the catalytic ozonation process with in-situ alternative backflushing exhibited a stable COD removal efficiency (above 45.6%) for 885 days when water- and air-flushing strengths of 10 L m s and 15 L m s, respectively, were applied with a 7-day regeneration interval. Therefore, the results of this study provide new insights into catalytic ozonation and support its engineering application in BCW treatment.
在这项研究中,使用中试和全规模系统研究了催化臭氧化法在处理生物处理焦化废水(BCW)中的性能。此外,还分析了 BCW 中有机污染物的去除效率、MnCeO/γ-Al2O3 的失活机制以及原位催化剂再生的反冲洗优化,这些都没有被之前的研究涉及到。12 个月的中试实验结果表明,当反冲洗作为原位催化剂再生策略时,催化臭氧化导致有机污染物的有效去除。出水化学需氧量(COD)含量从 150 降至 78mg/L,且低于 80mg/L 的排放标准,稳定的 COD 去除效率(从 56.0%降至 47.9%)表明,催化剂失活主要是由于无机盐在催化剂表面的沉积,限制了臭氧与活性位的相互作用和/或阻止了电子转移,主要通过反冲洗得到抑制。通过原位空气和水反冲洗实现的催化剂再生归因于冲洗、碰撞和/或松动效应。此外,在全规模实验中,当分别采用 10L/m·s 和 15L/m·s 的水和空气冲洗强度,以及 7 天的再生间隔时,原位交替反冲洗的催化臭氧化过程在 885 天内表现出稳定的 COD 去除效率(高于 45.6%)。因此,这项研究的结果为催化臭氧化提供了新的见解,并支持其在 BCW 处理中的工程应用。