Li Xuemei, Liu Yang, Guo Rui, Li Zicheng, Hu Qingming, Liu Meng, Zhu Lei, Kong Xiangxia
School of Mechanical and Electronic Engineering, Qiqihar University, Qiqihar 161006, China.
CRRC Qiqihar Rolling Stock Co., Ltd., Qiqihar 161002, China.
Materials (Basel). 2024 Mar 4;17(5):1198. doi: 10.3390/ma17051198.
In this paper, the corrosion environment of a railway coal truck was simulated with 1.0%HSO + 3%NaCl solution. The effect of weld toe Tungsten Inert Gas (TIG) remelting on the microstructure and corrosion resistance of welded joints of Q450NQR1 high-strength weathering steel was studied. The results show that the weld toe melts to form a remelting area after TIG remelting. After TIG remelting, the weld geometry was improved, and the stress concentration factor decreased from 1.17 to 1.06 at the weld toe, a decrease of 9.4%. TIG remelting refines the microstructure of the weld toe and improves the corrosion resistance of the welded joint. The surface of the TIG-remelted sample is uniformly corroded with no "deep and narrow" pits after the removal of corrosion products. The weight loss rate and corrosion rate of remelted welds are lower than those of unremelted welds. The structure of corrosion products is loose at the initial stage of corrosion, and the corrosion products are transformed into FeO and FeO protective rust layers with a dense structure after 480 h of corrosion. With the extension of corrosion time, the tensile strength and percentage elongation of the specimen decreased linearly. The decreasing rates of tensile strength of remelted and unremelted specimens were 0.09 and 0.11, respectively, and the decreasing rates of elongation after fracture were 0.0061 and 0.0076, respectively.
本文采用1.0%H₂SO₄ + 3%NaCl溶液模拟铁路运煤车的腐蚀环境。研究了焊趾钨极惰性气体(TIG)重熔对Q450NQR1高强度耐候钢焊接接头组织和耐蚀性的影响。结果表明,TIG重熔后焊趾熔化形成重熔区。TIG重熔后,焊缝几何形状得到改善,焊趾处的应力集中系数从1.17降至1.06,降低了9.4%。TIG重熔细化了焊趾组织,提高了焊接接头的耐蚀性。去除腐蚀产物后,TIG重熔试样表面均匀腐蚀,无“深而窄”的蚀坑。重熔焊缝的失重率和腐蚀速率低于未重熔焊缝。腐蚀初期腐蚀产物结构疏松,腐蚀480 h后腐蚀产物转变为结构致密的FeO和Fe₃O₄防护锈层。随着腐蚀时间的延长,试样的抗拉强度和伸长率呈线性下降。重熔和未重熔试样的抗拉强度下降速率分别为0.09和0.11,断后伸长率下降速率分别为0.0061和0.0076。