Nejad Peyman Ghashghaie, Zenouz Reza Taghavi
School of Mechanical Engineering, Iran University of Science and Technology (IUST), Narmak, Tehran, 16846-13114, Iran.
Sci Rep. 2023 Dec 19;13(1):22567. doi: 10.1038/s41598-023-49391-9.
Blades tip leakage flow structure in axial compressors has dominant effects on flow stability and losses. Accordingly, in the present study, three different ideas are introduced for alleviation of undesirable effects of the blades tip leakage flow. These ideas utilize circumferential tape, S-shape nozzle and natural aspiration slot, all imposed upstream the rotor blades row. The method of investigation is based on numerical simulation of the governing flow field. Results, in terms of the flow field structure and performance curves are compared with those of the untreated case. Final results, showed that the natural aspiration idea works better than the other ones. In comparison to the plane case, it is accompanied by augmentation of 3.5% in the total pressure ratio and 3% in the surge margin. It was also found that the mass flow rate passing through the blades row tip gap has increased by 2.33 g/s in the natural aspiration case.
轴流压气机叶片顶部泄漏流结构对流动稳定性和损失有显著影响。因此,在本研究中,引入了三种不同的方法来减轻叶片顶部泄漏流的不良影响。这些方法分别利用周向带、S形喷嘴和自然吸气槽,均施加在转子叶片排的上游。研究方法基于对控制流场的数值模拟。将流场结构和性能曲线方面的结果与未处理情况的结果进行了比较。最终结果表明,自然吸气方法比其他方法效果更好。与平面情况相比,总压比提高了3.5%,喘振裕度提高了3%。还发现,在自然吸气情况下,通过叶片排顶部间隙的质量流量增加了2.33 g/s。