Tian Guoliang, Ding Zhengjiang, Liu Baolin, Shang Zhenhua, Zhao Ke, Jiang Xin
China University of Geosciences (Beijing), Beijing 100083, China.
Geology and Mineral Exploration and Development Bureau (Sixth Geological and Mineral Exploration Institute of Shandong Province), Weihai, Shandong 265400, China.
ACS Omega. 2025 Aug 5;10(32):35907-35915. doi: 10.1021/acsomega.5c03040. eCollection 2025 Aug 19.
Traditional vertical shaft drilling rigs often suffer from inconsistent speed regulation, high energy consumption, and excessive noise. To address these challenges, this work proposes a frequency conversion control scheme and validates its feasibility through theoretical analysis and experimental testing. The retrofit employs a variable frequency drive to enable stepless speed adjustment, allowing dynamic control of the motor input frequency and voltage. This results in continuously variable speed regulation, significantly enhancing the drilling efficiency and adaptability to diverse geological conditions. By optimizing load characteristics, the system achieves substantial energy savings, with field tests demonstrating over 35% reduction in electricity usage compared with the original model. For an annual operation of 10 months, this translates to estimated savings of 62,742 kWh. Additionally, the average noise level of the retrofitted motor decreases from 94.28 to 89.51 dB, falling below the 90 dB occupational noise exposure limit. The upgraded electronic control system also incorporates multiple safety features, including overcurrent and overvoltage protection, reducing operational risks. These test-verified results of the inverter-based retrofit demonstrate its potential to advance traditional drilling rigs toward greater efficiency, intelligence, and sustainability, offering valuable technical insights for modernizing geological drilling equipment.
传统的立轴钻机经常存在调速不一致、能耗高和噪音过大的问题。为应对这些挑战,本文提出了一种变频控制方案,并通过理论分析和实验测试验证了其可行性。改造采用变频驱动器实现无级调速,可动态控制电机输入频率和电压。这实现了连续可变的速度调节,显著提高了钻探效率以及对不同地质条件的适应性。通过优化负载特性,该系统实现了大幅节能,现场测试表明与原型号相比,用电量减少了35%以上。以每年运行10个月计算,这意味着估计可节省62,742千瓦时。此外,改造后电机的平均噪音水平从94.28分贝降至89.51分贝,低于90分贝的职业噪音暴露限值。升级后的电子控制系统还具备多种安全功能,包括过流和过压保护,降低了运行风险。基于逆变器改造的这些经测试验证的结果表明,其有潜力推动传统钻机向更高效率、智能化和可持续性发展,为地质钻探设备现代化提供了有价值的技术见解。