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啤酒酿造行业中全尺寸上流式厌氧污泥床(UASB)反应器的性能

Full scale UASB reactor performance in the brewery industry.

作者信息

Ahn Y H, Min K S, Speece R E

机构信息

Department of Civil and Environmental Engineering, Vanderbilt University, P.O Box 1831, Station B, Nashville, TN 37235, USA.

出版信息

Environ Technol. 2001 Apr;22(4):463-76. doi: 10.1080/09593332208618276.

Abstract

In this paper the 7 year experience of the Oriental Breweries, located in Kumi, Korea utilizing a full-scale upflow anaerobic sludge blanket (UASB) reactor for the anaerobic pretreatment of brewery wastewater is presented. The anaerobic pretreatment system selected has successfully achieved the desired treatment efficiency for the brewery wastewater during that period and it has also continued operation even with low wastewater concentrations (average CODcr 1,400 mg l-1) and lower flow rates than specified by the design parameters. The CODcr removal of the UASB reactor averaged over 80% throughout the entire period, incurring normal running expenses of only $0.20-0.31 m-3 of treated water. In addition a further economical feature of the process was the utilization of the gas digester production as the municipal gas source, reducing total operating expenses around 30 to 45% and costing the plant only $0.1 m-3. Maintenance of good granule production, which is always a key issue in operating UASB systems, was not possible by this installation, however, so frequent expensive reseeding of the reactor was often necessary due to biomass washout. The full scale and lab scale research revealed that underloading can be as detrimental as overloading, due to excessively long retention time in the UASB system for the overall operating period and to excessive pre-acidification and/or incorrect reactor configuration of the completely mixed type. To enhance the sludge granulation, therefore, the installation of a pre-acidification reactor in the UASB system treating easily biodegradable substrates such as brewery wastewater is not necessary because adequate pre-acidification can occur in the equalization tank.

摘要

本文介绍了位于韩国龟尾市的东洋啤酒厂利用全尺寸上流式厌氧污泥床(UASB)反应器对啤酒厂废水进行厌氧预处理的7年经验。在此期间,所选的厌氧预处理系统成功实现了对啤酒厂废水的预期处理效率,并且即使在废水浓度较低(平均化学需氧量为1400mg/L)和流量低于设计参数规定的情况下,该系统仍能持续运行。在整个期间,UASB反应器的化学需氧量去除率平均超过80%,处理水的正常运行费用仅为每立方米0.20 - 0.31美元。此外,该工艺的另一个经济特点是将沼气池产生的气体用作城市燃气源,使总运营费用降低了约30%至45%,工厂成本仅为每立方米0.1美元。然而,该装置无法维持良好的颗粒污泥生成,而这在运行UASB系统时始终是一个关键问题,因此由于生物质流失,经常需要频繁且昂贵地重新接种反应器。全尺寸和实验室规模的研究表明,由于在整个运行期间UASB系统中的停留时间过长,以及完全混合式反应器的过度预酸化和/或配置不正确,低负荷可能与高负荷一样有害。因此,为了增强污泥颗粒化,在处理如啤酒厂废水等易生物降解底物的UASB系统中,不需要安装预酸化反应器,因为在均衡池中可以发生充分的预酸化。

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