Li Guo-Dong, Li Xin-Lei, Huan Heng-Heng, Lin Hai-Xiao, Ren Zi-Yuan, Ren Hao
School of Safety Engineering, China University of Mining and Technology, Beijing, 100083, China.
Jiaozuo Coal Industry (Group) Co., LTD, Jiaozuo, 454000, Henan, China.
Sci Rep. 2025 May 31;15(1):19158. doi: 10.1038/s41598-025-04268-x.
This study addresses hydraulic support resistance determination in deep coal pillar caving faces at Zhaogu No. 2 Mine through integrated theoretical, numerical, and field analyses. Theoretical calculations (empirical estimation: ≥ 15.742 MN; dynamic load coefficient: ≥ 10.975 MN) and a "cantilever beam-masonry beam" composite mechanical model (≥ 16.029 MN) defined the resistance range. Numerical simulations revealed progressive coal pillar stress increase during mining, with stress transitioning from bimodal to unimodal distributions due to superimposed abutment pressure and open-cut stress. Complete pillar failure at 5 m from the open-cut reduced roof capacity, while roof displacement analysis identified 1.8 MPa (16.569 MN resistance) as optimal support intensity. Similarity model experiments validated stress field consistency under 1.8 MPa, confirming effective roof control. Field implementation of ZF18000/21/38D supports demonstrated normal resistance distribution during operation, aligning with theoretical predictions. This framework offers critical guidance for deep coal pillar face support design.
本研究通过综合理论、数值和现场分析,探讨了赵固二矿深部煤柱放顶煤工作面的液压支架阻力确定问题。理论计算(经验估算:≥15.742 MN;动载系数:≥10.975 MN)和“悬臂梁-砌体梁”复合力学模型(≥16.029 MN)确定了阻力范围。数值模拟表明,开采过程中煤柱应力逐渐增加,由于叠加支承压力和开挖应力,应力从双峰分布转变为单峰分布。距开挖面5 m处煤柱完全破坏,降低了顶板承载能力,而顶板位移分析确定1.8 MPa(16.569 MN阻力)为最佳支护强度。相似模型试验验证了1.8 MPa下应力场的一致性,证实了有效的顶板控制。ZF18000/21/38D支架的现场应用表明,运行期间阻力分布正常,与理论预测一致。该框架为深部煤柱工作面支护设计提供了关键指导。